Hello Folks,
I have a 2000 model year 196 with the GT40 engine. Recently I discovered that the crankcase was 3-4 quarts over full. It almost certainly is fuel because the oil looks normal but is very thin (not brown/tan in color and not foamy) and no water separated from the oil when left in a glass jar for several days. It also has started idling fairly roughly. Sometimes when you bring the power back to idle abruptly, it will stall. At higher power settings it seems to run normally.
I have done the following:
1. Replaced all 8 fuel injectors with new 24 lb Ford Performance injectors.
2. Scanned the computer for failure codes. No codes are present.
3. Checked fuel pressure with a gage. Readings are normal per PCM maintenance manual.
4. Checked vacuum line from pressure regulator to plenum for fuel (temporarily replaced the vacuum hose with a clear hose to visualize any fuel getting sucked into the plenum). No fuel in line.
5. Checked injectors with a stethoscope at idle. All injectors can easily be heard clicking on and off.
6. Changed the plugs.
7. Measured resistance in plug wires with ohm meter accounting for wire length. All wires well within specs per PCM maintenance manual.
After accomplishing the above, I changed the oil and filter and ran the boat for about 1.5 hours over a weekend. After that time the dipstick showed the crankcase over full by about 1 inch (roughly 1 quart). Has anyone seen this happen? Any thoughts would be appreciated!
Bruce
I have a 2000 model year 196 with the GT40 engine. Recently I discovered that the crankcase was 3-4 quarts over full. It almost certainly is fuel because the oil looks normal but is very thin (not brown/tan in color and not foamy) and no water separated from the oil when left in a glass jar for several days. It also has started idling fairly roughly. Sometimes when you bring the power back to idle abruptly, it will stall. At higher power settings it seems to run normally.
I have done the following:
1. Replaced all 8 fuel injectors with new 24 lb Ford Performance injectors.
2. Scanned the computer for failure codes. No codes are present.
3. Checked fuel pressure with a gage. Readings are normal per PCM maintenance manual.
4. Checked vacuum line from pressure regulator to plenum for fuel (temporarily replaced the vacuum hose with a clear hose to visualize any fuel getting sucked into the plenum). No fuel in line.
5. Checked injectors with a stethoscope at idle. All injectors can easily be heard clicking on and off.
6. Changed the plugs.
7. Measured resistance in plug wires with ohm meter accounting for wire length. All wires well within specs per PCM maintenance manual.
After accomplishing the above, I changed the oil and filter and ran the boat for about 1.5 hours over a weekend. After that time the dipstick showed the crankcase over full by about 1 inch (roughly 1 quart). Has anyone seen this happen? Any thoughts would be appreciated!
Bruce
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